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Sound measurements on a 4000-pound-thrust high-bypass-ratio turbofan engine
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The article was published on 1970-03-01 and is currently open access. It has received 2 citations till now. The article focuses on the topics: Bypass ratio & Jet engine.read more
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Effects of casing boundary-layer removal on noise of a turbofan rotor
TL;DR: In this article, the effect of casing boundary layer removal on noise produced by a turbofan rotor was measured, and the results showed that overall sound pressure level was reduced 2 dB with moderate blade loading and 3 dB with heavier blade loading.